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November 21, 2019

Gearbox

[All the pics are clickable]

The gearbox in my GT6 was a pretty ordinary non-overdrive four speed unit with synchromesh in all four gears.

First job was to divorce the box from the engine and get it down to the shop.  There was an abandoned critter household in the bell housing.




The GT6 gearbox assembly is made up of five subassemblies:  

the gearbox itself, where all the gears are,
the bell housing, which encloses the clutch and flywheel,
the tail extension, which supports the rear of the output shaft and includes the speedometer drive,
the gear selector, which coordinates gear selection and prevents more than one gear at a time being engaged, and
the remote control, which puts the shift lever within easy reach of the driver.




I started at the top, with the remote control assembly.  To jump directly to the gearbox itself, click here.




The first thing I norticed about the remote control was that the selector lever was very loose and sloppy.  Taking it apart, there appeared to be at least one part missing.




There is a kit of parts available to tighten up the lever, so I ordered one.  The missing part was the nylon half-ball that fits at the base of the lever, and rides in a spherical socket in the housing.  The ball in the kit was pretty rough, with pretty pronounced casting flash.  It didn't ride very smoothly in the socket.  It took a little work to clean it up, and it then worked fine.




A few of the other parts in the kit were sort of disappointing.  I ended up replating and re-using this original retainer rather than the new one (new one on the left).




For the rest of the parts, I used a mix of the old and new, whichever worked better.  I powder coated most of the exposed parts, including the aluminum housing.




The square-head bolt that retains the selector finger was actually a lock bolt, with a little nylon pellet inserted in the threaded portion.  Like "Nylok" nuts, these really shouldn't be re-used.  I didn't really want to wait (or pay) for a new bolt, so I found some 1/8" nylon rod and just made a new insert.




This is all the moving parts assembled except fot the shift lever.




This is the reverse lockout tab, which makes it harder to accidentally shift into reverse.




Then the shift lever was installed.  It now works firmly but smoothly.




The shift lever on the remote control manipulates internals of the gear selector assembly, which in turn moves parts inside the gearbox.  It moves those parts by way of bronze selector forks.




The forks are attached to three rods that can move fore and aft, controlled by motion from the shift lever.  One rod controls first and second gears, another controls third and fourth, and the third rod controls reverse.




I like to linish mating machined surfaces on a plate to make sure they are flat.




Here are all of the parts cleaned and inspected, and the housing powder coated.  The selector assembly includes an interlock mechanism to prevent more than one rod and selector fork from moving at the same time.  This would cause more than one gear to be engaged, which would be confusing for the gearbox.  The little pin and ball on the right side of the picture are part of the interlock.  All of the parts listings I saw only called for one ball, but two are actually required for full interlock.




The selector assembly also provides fairly strong spring loaded detents for each rod, which provide a good positive feel for shifting, and also ensure that the gearbox won't pop out of gear.  The more blunt detent is for the reverse rod.




Here is everything put back in the housing.  The forks are attached by three more of those square head lock bolts that got new nylon buttons.  The third picture shows the slot that the finger from the remote control fits into..




The bores that the three control rods slide in are open at both ends of the housing.  They have to be closed off with small core plugs.  I'm not sure what the LBC suppliers have, but these came from an industrial supplier, and were not plated.  A quick zinc plate fixed that right up.




This is the reverse switch which controls the backup lights.  A test with an ohmmeter showed that it was not working.  I didn't thiink I had a lot to lose by trying to fix it.




It was pretty grody inside, apparently from leaked oil., but the parts cleaned up well.




This O ring on the actuator button was hard and cracked, and surely the source of the leaked oil.  It's a standard size O ring.




All renewed and reassembled, and it worked!




Cleaned and replated the original studs, and this piece is ready.




The tailpiece is simpler than the shifter subassemblies.  After pulling everything out of it, the casting was cleaned up, linished, and powder coated.




The speedometer drive assembly got a new seal and O ring.  That little stepped rod is a thrust seat that goes in the housing to limit play of the gear.




The only other parts are the bearing and oil seal for the rear end.




The bell housing is the simplest assembly.  It was stripped, cleaned, and powder coated.  I had my doubts, but it did fit in my smallish oven, with probably a half an inch all around.




Then the nose piece was pressed in, then the oil seal.  The throwout bearing carrier will have to come out again to install the bearing.




And now to the main event.  Peering into a gearbox can be a little intimidating.  There are a lot of parts crammed in there, and the way they have to fit together is very often not intuitive.  I don't recommend anyone try this without at least two good manuals.  The factory manual is very good, but it mentions quite a few special factory tools which are difficult or impossible to find.  Non-factory manuals will often recommend techniques that don't require the factory tools.




So I gutted the gearbox, trying to keep things in order and in the correct orientation.




I cleaned and visually inspected each part, looking for damage or excessive wear.  I didn't really find anything worrisome, so I moved on.

There are a number of measurements mentioned in the manuals to determine if anything needs to be replaced or adjusted.  There are two synchronizer assemblies, one for first and second gears, and the other for third and fourth.  They have spring loaded detents in their central neutral position, and there is a spec for the amount of force it should take to unseat the detent balls.  Both of my synchronizers took about 20 pounds, which is within spec.




Next, measurement of the end float of the 2nd and 3rd gears on their bushings.  This is done on a flat plate with feeler gauges.  Mine came out at about 0.003, well within spec.




There were a couple of other measurements on the mainshaft to do, and they also came out within spec.  So far, this gearbox appeared to have very little wear.

At this point, I rounded up the reverse gear and shaft and put them in the case, mainly so they wouldn't walk away.




The next job was to install the laygear cluster with it's thrust washers to measure its endfloat.  The laygear runs on 25 loose needle bearings on each end.  To keep them from going AWOL, a temporary short layshaft has to be used to keep them contained.  I made a shaft from a length of 3/8" black iron pipe.




With the laygear cluster in place with its two thrust washers, and the temporary shaft replaced by the real one, I could measure the end float.  Again, it was within spec, so new thrust washers wouldn't be necessary.




Then the lay shaft was replaced by the shorter temporary one again.  This allows the laygear cluster to fall to the bottom of the case, leaving room for the mainshaft to go in.

I built up the mainshaft according to the manuals, and inserted it into the case.  Though the original bronze synch rings really looked fine, I bought new ones.  There seem to be two types available from suppliers.  Based on some sad stories I'd read, I got the more expensive ones.




Then I built the much simpler input shaft.  With all of the wear measurements so good, I probably could have just reinstalled the original main bearings, but I had ordered new ones, so I used them.  That little caged roller bearing fits in the end of the input shaft, and the nose of the main shaft goes into it.




So, now, with the main and input shafts and bearings all fully installed and rotating freely, I was home free.

Except.  When I rolled the case on its side, I heard a horrifying little clink, and out fell this special little item onto the bench.




It's a split washer that was supposed to be deep within the mainshaft assembly.

So, everything had to come out again to reinstall the split washer.  Finally got it back together, and turned the case upside down to see what would fall out.  Nothing.  Silence.  Beautiful!

Then, while in the middle of my fifth or sixth fist pump, I caught the glimmer of the shiny little fourth gear synch ring that should have been installed with the input shaft.




I was relieved to realize that this part could be installed by only removing the input shaft.  I was getting pretty good at that.

OK, so after scouring the bench and the surrounding floor for loose parts, I finally decided that everything that is supposed to be in the case was in there.

I pulled the lay cluster gear up into mesh with the main and input shafts, and used the layshaft to push out the temporary shaft. This is when it is a good idea to make sure everything still turns like it should, and that all of the gears work.  

Lastly, I pushed on the spiral gear for the speedometer drive.





So, here are all of the subassemblies ready for the mating ceremony.  Where I can, I replate and re-use the original hardware.  




Bell housing and tailpiece on.




Gear selector and remote control.




And finally, the drive flange.




I checked out all the gears for proper and smooth operation, and am now satisfied that the gearbox is probably together correctly.




This was sort of a harrowing project.  I have done exactly one gearbox before, and it hasn't really gotten any easier.  

Though in hindsight, and with the benefit of all the internal measurements, I may not have had to replace much in this gearbox, I did replace the bearings , seals, and synch rings, which came to something under $250

Comments to Ed at elhollin1@yahoo.com.  

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